The remediation oil production by matrix acidizing method on the well named "X" (for confidential reasons) is scrutinized in this paper. Initial production of 1150 bpd, production index of 2.8 STB/Psi/d and permeability of 150md, in 2018 two years down the lane this dropped to 450 bpd, production index 0.7 STB/Psi/d. The declined observed on the production index is trouble shouted and after elimination of (no completion damage/perforation damage), the skin is calculated by carrying out a well test (build-up test) whose extrapolation in excel over times gave us a skin of 40.The reservoir heterogeneity, containing >20% of feldspar, carbonates and paraffin’s guided thematrix acidizing design and treatment proposition to remedy this problem. A positive displacement pump (HT400), boosted by a centrifugal pump were used to pump the acid treatment through high pressure treating line downhole. Halliburton insite for stimulation the (IFS) software monitored treating pressure and surface flow rate, keeping injection rate below fracturing pressure. PipeSim software is used to run the nodal analysis before and after treatment this helped to forecast optimal production rates and pressure after treatments. Matrix acidizing method applied on the well X increased the production to 850 bpd with production index of 2 STD/psi/d, skin - 1.5. The economic benefit to the company stood at (profit oil 21,699,500 USD.) over a two years period of production. Meanwhile uncertainties in demand and supply of crude oil at the international market cause constant fluctuation in oil prices, this should be strongly considered upon execution of this project. Overall applications of this acidizing treatment can be carried out on reservoirs with similar mineralogy. HCl/HF blend dissolves sandstone, mud stone and calcite minerals thus reservoir porosity and permeability can be enhanced in regions extending several meters around the injection well.
This work studies with produce of light fuel fractions of gasoline, kerosene and gas oil from treatment of residual matter that will be obtained from the solvent extraction process as by product from refined lubricate to improve oil viscosity index in any petroleum refinery. The percentage of this byproduct is approximately 10% according to all feed (crude oil) in the petroleum refinery process. The objective of this research is to study the effect of the residence time parameter on the thermal cracking process of the byproduct feed at a constant temperature, (400 °C). The first step of this treatment is the thermal cracking of this byproduct material by a constructed batch reactor occupied with control device at a selective range of re
... Show MoreThe present research has investigated the effect of microwave energy on improving the flow properties of heavy crude oil. The fragmentation of crude oil molecules was carried out with and without using 1 and 10 wt. % concentration of various types of H-donors like tetralin, cyclohexane, and naphtha. Microwave power of 320, 385, and 540 W and radiation time 1-9 min, and temperature were studied. The kinematic viscosity and asphaltene content were measured for evaluation the improving of heavy crude oil.
Results show that viscosity of crude oil decreased with increase H-donor concentration, a maximum percentage of viscosity reduction was10.63 % for tetralin at 6 min radiation time, while 8.67%, and 7.34% for cycl
... Show MoreThis research was aimed to study the efficiency of microfiltration membranes for the treatment of oily wastewater and the factors affecting the performance of the microfiltration membranes experimental work were includes operating the microfiltration process using polypropylene membrane (1 micron) and ceramic membrane (0.5 micron) constructed as candle; two methods of operation were examined: dead end and cross flow. The oil emulsion was prepared using two types of oils: vegetable oil and motor oil (classic oil 20W-50). The operating parameters studied are: feed oil concentration 50 – 800 mg/l, feed flow rate 10 – 40 l/h, and temperature 30 – 50 oC, for dead end and cross flow microfiltration.
It was found that water flux decrea
Smart water flooding (low salinity water flooding) was mainly invested in a sandstone reservoir. The main reasons for using low salinity water flooding are; to improve oil recovery and to give a support for the reservoir pressure.
In this study, two core plugs of sandstone were used with different permeability from south of Iraq to explain the effect of water injection with different ions concentration on the oil recovery. Water types that have been used are formation water, seawater, modified low salinity water, and deionized water.
The effects of water salinity, the flow rate of water injected, and the permeability of core plugs have been studied in order to summarize the best conditions of low salinity
... Show MoreThis paper addresses the factors responsible for changes in crude oil prices, in real market and financial sector. In order to prepare the analytical background for further investigation, it highlights the patterns of correlations of the real oil price and the most related prices of assets, exchange rate and government bond yield. The paper reviews the statistical behavior of oil price, quantities and the global macroeconomic environment. Topics discussed include the theory of differential rent and scarcity effect ,the role of future market and speculation, strategies of energy of the major economies to investigate the prospects of oil market and the potential demand for OPEC's oil. The paper explores the
... Show MoreA modified water injection technique has organized by this study to improve oil recovery of the Mishrif reservoirs using polymerized alkaline surfactant water (PAS-Water) injection. It is planned to modify the existing water injection technology, first to control and balance the hazardous troublemaker reservoir facies of fifty-micron pore sizes with over 500 millidarcies permeability, along with the non-troublemaker types of less than twenty micron pore sizes with 45 to 100 millidarcies permeability. Second to control Mishrif reservoirs rock-wettability. Special core analysis under reservoir conditions of 2250 psi and 90 °C has carried out on tens of standard core plugs with heterogeneous buildup, using the proposed renewal water f
... Show MoreMany oil and gas processes, including oil recovery, oil transportation, and petroleum processing, are negatively impacted by the precipitation and deposition of asphaltene. Screening methods for determining the stability of asphaltenes in crude oil have been developed due to the high cost of remediating asphaltene deposition in crude oil production and processing. The colloidal instability index, the Asphaltene-resin ratio, the De Boer plot, and the modified colloidal instability index were used to predict the stability of asphaltene in crude oil in this study. The screening approaches were investigated in detail, as done for the experimental results obtained from them. The factors regulating the asphaltene precipitation are different fr
... Show More Aluminum alloys widely use in production of the automobile and the aerospace because
they have low density, attractive mechanical properties with respect to their weight, better
corrosion and wear resistance, low thermal coefficient of expansion comparison with traditional
metals and alloys. Recently, researchers have shifted from single material to composite materials
to reduce weight and cost, improve quality, and high performance in structural materials.
Friction stir processing (FSP) has been successfully researched for manufacturing of metal
matrix composites (MMCs) and functional graded materials (FGMs), find out new possibilities
to chemically change the surfaces. It is shown th
A laboratory investigation of six different tests were conducted on silty clay soil spiked with lead in concentrations of 1500 mg/kg. A constant DC voltage gradient of 1 V/cm was applied for all these tests with duration of 7 days remediation process for each test. Different purging solutions and addition configurations, i.e. injection wells, were investigated experimentally to enhance the removal of lead from Iraqi soil during electro-kinetic remediation process. The experimental results showed that the overall removal efficiency of lead for tests conducted with distilled water, 0.1 M acetic acid, 0.2 M EDTA and 1 M ammonium citrate as the purging solutions were equal to 18 %, 37 %, 42 %, and 29 %, respectively. H
... Show MoreThe permeable reactive barrier (PRB) is one of the promising innovative in situ groundwater remediation technologies, in removing of copper from a contaminated shallow aquifer. The 1:1- mixture of waste foundry sand (WFS) and Kerbala’s sand (KS) was used for PRB. The WFS was represented the reactivity material while KS used to increase the permeability of PRB only. However, Fourier-transform infrared (FTIR) analysis proved that the carboxylic and alkyl halides groups are responsible for the sorption of copper onto WFS. Batch tests have been performed to characterize the equilibrium sorption properties of the (WFS+KS) mix in copper- containing aqueous
solutions. The sorption data for Cu+2 ions, obtained by batch experiments, have be